i did mention the throttle slide earlier on in thread.
sometimes they are put in the wrong way- so that leaves a gap when it should be closed.guilty of it myself in the past -resulting in engine revving ike a maniac
Putting it in the wrong way leaves it open about half way haha
I know there's some right bodges on this bike and its taken the piss to sort them. It ran like this on the other carb aswell before I stripped it.
I'm going to have to have a proper look, I'll keep you posted
if t did the same with 2 diff carbs then I think we can say its not the carbs .
when you changed carbs did you change all the carb or keep the same top and slider / needle with same cable on each time ?
maybe remove cable from carb altogether and test it that way use a bit of string if need be to lift slider a little if need be it will eliminate cable for problems .
That shouldnt lead you to think that. If you throttle a bike thats cold on choke it will die. You're giving the engine the complete wrong mixture that it needs to combust. Thats all caused by the carb.
I still say its air leak maybe at pv or cable problem .
wheres that other topic just like this we went on for weeks saying all the same things with the owner saying he did this and did that then in the end it all came down to the cable trapped/pinched or routed wrong .. just by passing the rev cable around the frame wrong or squished in tight behind lights or wires can cause this..
done it myself and on one bike it would rev high if I turned left was fun on corners lol
You should start it with choke if needed then turn off asap. Then let it warm up before revving it much.
The slide should be completely closed. It's really not difficult to take the carb off. remove the slide from the cable and drop it in. You'll see how far it should go down and see that it closes fully.
You've also told us that the bore has scores in and the old piston has gone back in. Without starting to remove the possible causes of the problem im not sure how you're expecting to fix the problem. Theory is all well and good but put the ideas that we are suggesting into practice. I know its frustrating to go back over the same things you say you have checked but we all make mistakes. you may well find something that you hadnt noticed the previous times.
My suggestions are
compression test- if low, rebore and piston kit
if good compression...
...remove carb and check the slide can return fully.
If it doesn't then youre throttle cable is probably wrong.
You should start it with choke if needed then turn off asap. Then let it warm up before revving it much.
The slide should be completely closed. It's really not difficult to take the carb off. remove the slide from the cable and drop it in. You'll see how far it should go down and see that it closes fully.
You've also told us that the bore has scores in and the old piston has gone back in. Without starting to remove the possible causes of the problem im not sure how you're expecting to fix the problem. Theory is all well and good but put the ideas that we are suggesting into practice. I know its frustrating to go back over the same things you say you have checked but we all make mistakes. you may well find something that you hadnt noticed the previous times.
My suggestions are
compression test- if low, rebore and piston kit if good compression...
...remove carb and check the slide can return fully. If it doesn't then youre throttle cable is probably wrong.
Yh get what your saying, the bikes in someone else's garage and I've only the weekend to work on it as I don't have the keys . Hence why I haven't got anywhere or tried anything.
I watched slobs video and thats pretty much how it sounds except I didn't let mine go past 5k, I bet it is throttle cable.
So this is what happened, choke being on unless stated.
Kicked it over a few times, wouldn't start
Turned idle in a bit screw, started after a few kicks and died
Kicked it again and it started then revved to about 4k and turned the choke to settle it about 3k. Let the bike warm up and gradually turned the choke down. Got to about 1.8k and with the smallest amount of choke, every so often it would sound like it was going to die so I turned the choke up a bit and back down to let it settle again. I had it running like this until it got quite hot at least running temp but it still wouldn't want to idle. Then it died with no word of warning
Started it again with choke fully on and it would still rev up like mad, I let it get to 7k before backing off and it slowly settled like previous.
Started it again and it wouldn't want to settle and now it doesn't want to start.
-- Edited by mr karnage on Saturday 25th of January 2014 05:19:52 PM
Whaaaa? dude. get the bike running as it should and ride it a bit before you start machining the head for or rings. You've probably spent more time on here that it would take to whip the barrel the off and check the clearances and condition of the bore and piston/rings. You dont need a tighter squish clearance or o ring head gaskets. you need a good seal between the rings and the bore and a genuine/athena head gasket.
Tighter squish. Yeah brilliant. It's great in theory in practice. Mate not being funny but you wouldn't last long.
If you machine the head down to OEM specifications you have to be so meticulous with the build.
There is a reason why Yamaha don't machine it down properly. Because they allow for human/machine error. Let's say that the squish clearance is bang on. If the connecting rod stretches any more than it's suppose to you will hit the head. Let's assume that doesn't happen. But you put a new piston in. Tell me honestly. Have you ever measured the dimensions of a piston to make sure that its height is exactly the right size. If it's any bigger you will again hit the head. Even if that's not the case. Let's say again the squish clearance is perfect. But you over torque the head nuts. Again you risk hitting the head.
The clearance is purposely bad to allow errors during the build to take place. The wrong mismatch between too much stretching of a connecting rod and too tall a piston still allows the bike to be within tolerances.
O-rings are great for race engines BECAUSE THEY WILL CHECK ALL THESE MEASUREMENTS. And if you intend to do so then fair play. That ought to pay off for you. But if like me you check the basics and bash it together then just leave it as it is.
Yes I knew that and after checking the squish clearance I don't need to have it reduced and as far as getting it machined to take o rings the original head gasket is measured then the head is machined and the squish is set last so your running the same clearance as before but with o rings. standard squash ranges at about 1mm to 1.2mm reducing it to .7 Isn't exactly race tolerances
Do you really think it's a bad idea?
On the piston and bore, the piston had signs of blow by at the sides and particularly at the second ring end gap. The cylinder definatley needs a rebore
As far as the o ring goes i dont understand why you want to? You know your compression isnt running too high as the head gaskets arent failing. You also know your compression is in fact low. You know the barrel needs rebore and the piston has blow by marks. Why are you trying to find another cause for your issues when you havnt address the most obivous one that you already knew about when you built the engine. round and round and round in circles we go...